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wfjm.w11/doc/README_known_issues.md
2022-09-03 09:12:51 +02:00

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Known issues

The case id indicates the release when the issue was first recognized.

V0.791-1 {issue #33} -- MMU: PDR A bit is set for every access

The PDR A bit is described in the Technical Manual as

A bit (bit 7) - This bit is used by software to determine whether or not
any accesses to this page met the trap condition specified by the Access
Control Field (ACF). (A = I is affirmative). The A bit is used in the
process of gathering Memory Management statistics.

It is set when the page ACF enables an MMU trap, thus for

  • ACF=1 and read access
  • ACF=4 and any access
  • ACF=5 and write access

The w11 currently sets the 'A' bit on any non-aborted access regardless of the ACF value.

No practical impact, the 'A' bit in PDR is a 11/45 11/70 only feature and not used in OS software.

V0.79-2 {issue #30} -- SimH scmd files fail on current 4.* version; only 3.* supported

The SimH scmd scripts were originally developed for SimH 3.8, and worked for SimH 3.9 and later releases. The SimH 4.* development team decided not to provide releases anymore, and over time this version became incompatible with the scmd scripts used for w11. That is most pronounced for the RT11 V4.3 oskit. A simple

  cd $RETROBASE/tools/oskit/rt11-53_rl
  console_starter -s -d DL0  &
  pdp11 rt11-53_rl_boot.scmd

works fine for SimH V3.9, V3.10 and V3.11-1, but fails

  • for pdp11-4.0-beta1 with core dump
  • for pdp11-2016-12-26-5ced037b with signal SIGSEGV in pdp11_xu
  • for pdp11-2019-07-28-2f707ffc with signal SIGSEGV in pdp11_xu
  • for pdp11-2020-03-26-261abfc3 with signal SIGSEGV in pdp11_xu
  • for pdp11-2021-08-22-64b12234 with signal SIGSEGV in pdp11_xu
  • for pdp11-2022-04-17-d3f1ee09 with with errors like
    • Device auto configuration is now disabled
    • Command not allowed (for set rha enabled)
    • container incompatible with the RL device

Bottom line:

  • the provided scmd scripts work only with SimH V3.9, V3.10 or V3.11-1
  • an update to the SimH V4.* has low priority

V0.50-2 {issue #28} -- RK11: write protect action too slow

Some simple RK11 drivers, especially in test codes, don't poll for completion of a write protect command. Due to the emulated I/O this can cause errors.

One example is the boot sequence of RK based XXDP, as seen for example for the dzzza disk. On SimH the disk is immediately switched to write protect mode, on w11 it is not. The pertinent part of the code is

    000214  B003:  mov	#000017,@#rk.cs   ; #rk.fwl+rk.go;  func=write_lock
    000222         bic	#017777,r2      
    000226         clc	
    000230         rol	r2
    000232         rol	r2
    000234         rol	r2
    000236         rol	r2
    000240         mov	r2,D040
    000244         mov	#000001,@#rk.cs   ; #rk.go;         func=control reset

The monitor does two writes to the RK11 CSR without busy polling and just a few instructions in between. In the w11 implementation the first write will set func=write_lock and cause an attn request. But before the attn can be serviced the CSR is overwritten with func=creset. The write lock is lost, only the creset is executed.

Can be resolved by handling write lock locally. Normal OS always do a busy poll before starting a function, therefore this is considered a minor deficit. Might be fixed in an upcoming release.

V0.50-3 {issue #27} -- CPU: no mmu trap when instruction which clears trap enable itself causes a trap

The MMU should issue an mmu trap if the instruction clearing the 'mmu trap enable' bit (bit 9 in mmr0) itself causes a trap. The 11/70 documentation clearly describes this behavior.

This is the reason why test 063 of the ekbee1 diagnostics currently fails.

Since the MMU trap mechanism is is only available on 11/45 and 11/70, but not in the J11, it is not used by common operating systems.

Therefore this is considered a to be a minor deficit. Will be fixed in an upcoming release.

V0.50-6 {issue #26} -- CPU: MMR0 trap bit set when access aborted

The MMU should set the 'trap bit' in MMR0 only when the access is not aborted. The current pdp11_mmu implementation sets the bit even when the access is aborted.

This is the reason why test 064 of the ekbee1 diagnostics currently fails.

Since the MMU trap mechanism is is only available on 11/45 and 11/70, but not in the J11, it is not used by common operating systems.

Therefore this is considered a to be a minor deficit. Will be fixed in an upcoming release.

V0.50-5 {issue #25} -- CPU: The AIB bit in MMU PDR register set independant of ACF field

The MMU should set the AIB A bit in the the PDR only when "trap condition is met by the Access Control Field (ACF)". Thus for

   ACF=001 read-only  trap on read
   ACF=100 read/write trap on read or write
   ACF=101 read/write trap on write

The current pdp11_mmu implementation always sets the bit, the logic is simply

    if doabort = '0' then
      AIB_SETA <= '1';
      AIB_SETW <= CNTL.wacc or CNTL.macc;
    end if;

Since the MMU trap mechanism is is only available on 11/45 and 11/70, but not in the J11, it is not used by common operating systems.

Therefore this is considered a to be a minor deficit. Will be fixed in an upcoming release.

V0.50-4 {issue #24} -- CPU: src+dst deltas summed in mmr1 if register identical

Test 12 of maindec ekbee1 fails because it expects after a

        mov    #100000,@#mmr0

which sets an error bit in mmr0 and thus freezes mmr0, that mmr1 contains

  013427 (00010 111 00010 111) (+2,r7;+2,r7)

while w11a gives

  000047 (00000 000 00100 111) (--,--;+4,r7)

The mmr1 content is different compared to the original 11/70 behavior, but is logically correct, fault recovery in OS (like in 211bsd) will work correctly. Therefore this is considered a to be a minor deficit.

The 11/70 documentation clearly states that there is an additional state bit that counts the write accesses to mmr1. This ensures that each of the two logged accesses end in separate bytes (byte 0 filled first).

The w11a only uses byte 1 when the register number differs.

V0.50-1 {issue #23} -- CPU: several deficits in trap logic

The current w11a implementation has several deficits in the handling of traps and interrupts which lead to non-conforming behavior when multiple trap, fault and interrupt conditions occur simultaneously, for example

  • bad stack frame when IOT trigger stack violation (TCK-003)
  • bad stack frame when interrupt triggers stack violation (TCK-004)
  • no yellow stack abort when jsr triggers a stack violation (TCK-006)
  • no odd address trap when EMT is executed with odd SP (TCK-007)
  • no yellow stack abort for mov (sp),(sp) (TCK-028)

These situations never occur during the execution of operation systems, and in case they do, the operating system will crash anyway. Thus there is no impact in normal usage, but diagnostics programs do complain. Will be fixed in an upcoming release.

V0.50-8 {issue #21} -- RK11,RL11: no proper NXM check in 18bit systems

No NXM error is generated when a UNIBUS device DMA transfer reaches the top of memory in 18 bit addressing. Seen originally for RK11, but RL11 and DEUNA are also affected.

In normal operation is minor non-conformity is not relevant because operating systems never set up DMA transfers to/from non-existing memory. However, some highly space optimized crash dump routines use this to detect end-of-memory and might endless loop. Also maindec's might test this border case and fail.

V0.76-3 {issue #18} -- w11 clock rate limited by CACHE-to-CACHE false path

So far all Series-7 w11a systems ran with 80 MHz clock. The sys_w11_arty design (with DDR memory support via MIG) also achieves timing closure under Vivado 2017.2, but fails (with a small negative slack) under Vivado 2018.3.

The failing data path has

  Source:      SYS70/CACHE/CMEM_DAT1/sv_ram_reg_0/DOADO[1]
  Destination: SYS70/CACHE/CMEM_DAT3/sv_ram_reg_0/DIADI[1]
  via            VMBOX->SEQ->OUNIT->SEQ->DPATH->SEQ->VMBOX

The connectivity of the multiplexers in pdp_dpath in principle allows such a data flow, but pdp11_sequencer will never configure the multiplexers in such a way. So technically this is a false path.

It seems that the placer strategy changed from Vivado 2017.2 to 2018.3 and that 2018.3 is less tolerant to the sub-optimal w11a design.

This will be fixed in a future release, either by setting up an appropriate false_path constraint, or by changing the data path structure.

V0.73-2 {issue #10} -- Many post-synthesis simulations fail

Many post-synthesis functional and especially post-routing timing simulations currently fail due to startup and initialization problems. Cause is MMCM/PLL startup, which is not properly reflected in the test bench. Will be resolved in an upcoming release.

V0.65-2 {issue #7} -- Some exotic RH70/RP/RM features not implemented

some exotic RH70/RP/RM features and conditions not implemented yet

  • last block transfered flag (in DS)
  • CS2.BAI currently ignored and not handled
  • read or write 'with header' gives currently ILF

All this isn't used by any OS, so in practice not relevant.

V0.65-1 {issue #6} -- ti_rri crashes in normal rundown in very rare cases

ti_rri sometimes crashes in normal rundown (exit or ^D) when a cuff: type rlink is active. One gets

      terminate called after throwing an instance of 'Retro::Rexception'
        what():  RlinkPortCuff::Cleanup(): driver thread failed to stop

Doesn't affect normal operation, will be fixed in upcoming release.

V0.64-6 {issue #5} -- IO delays still unconstraint in Vivado

IO delays still unconstraint in Vivado. All critical IOs use explicitly IOB flops, thus timing well defined.

rlink throughput on basys3/nexys4 limited by serial port stack round trip times. Will be overcome by libusb based custom driver.

rlink v4 error recovery not yet implemented, will crash on error.

rlink command lists aren't split to fit in retransmit buffer size.

{the last two issues are not relevant for w11 backend over USB usage because the backend produces proper command lists and the USB channel is usually error free}

Resolved Issues

V0.79-1 {issue #29} -- migrate from Travis to GitHub actions

Original Issue

Travis is now defunct and has been removed in 6b8c063. So it's time to migrate CI/CD to GitHub actions.

Fix

GitHub Actions fully implemented with commit db7556a4, fine tuned with commit 66f3f5d0.

V0.76-1 {issue #16} -- Help wanted: Testing with Nexys4 DDR appreciated

Original Issue

The w11a design for Nexys4 DDR, see rtl/sys_gen/w11a/nexys4d, was provided to support also an up-to-date Nexys4 board. It is so far only simulation tested.

Testing done with a real Nexyx4 DDR, or a newer Nexys A7-100T, would be highly appreciated. Please double check the pin assignments (see mig_a.prj and nexys4d*.xdc) with the documentation of your board to avoid potential damage.

Looking forward to receive test reports.

Fix

The Nexys4 (classic, with 16 MByte PSRAM) board, on which most of the recent w11 was done, broke in late July 2019 (see blog) and a Nexys A7 was ordered as replacement.

Basic tests with the test designs sys_tst_serloop2 and sys_tst_rlink_n4d and the BRAM-only w11 design sys_w11a_br_n4d worked fine.

But all tests involving the DDR2 memory interface failed. The culprit was quickly found, it was a mistake in the MIG configuration mig_a.prj, the polarity of the SYS_RST signal was ACTIVE LOW instead of ACTIVE HIGH. After fixing this, the test designs sys_tst_mig_n4d and sys_tst_sram_n4d as well as the w11 implementation sys_w11a_n4d worked right away.

The tst_sram designs show nicely that the DDR2 on the Nexys A7 board is slightly slower than the DDR3 on the Arty A7 board

   Board     test time   clock period     UI_CLK
  Nexys A7     37.36 s        3333 ps   75.0 MHz 
  Arty A7      35.77 s        3000 ps   83.3 MHz

Closed with commit 563e230.

V0.66-1 {issue #8} -- TM11 controller doesn't support odd transfer size

Original Issue

The TM11 controller transfers data byte wise (all disk do it 16bit word wise) and allows for odd byte length transfers. Odd length transfers are currently not supported and rejected as invalid command. Odd byte length records aren't used by OS, so in practice this limitation isn't relevant.

Fix

Odd record length support added with commit 5b52e54.

V0.742-1 {issue #14} -- SEGFAULT core dump after detach

Original Issue

The detach of a tcp type virtual terminal or a tap type virtual ethernet device can lead to a SEGFAULT core dump, e.g. after a cpu0ttb0 det command. This is caused by a race condition between the detach run-down and the implementation of ReventLoop::RemovePollHandler().

Fix

The culprit was a design error in the RemovePollHandler flow, which allowed that DoPoll returned while poll list updates were still pending and the subsequent execution of DoCall called removed handlers. DoPoll now loops until there are no pending poll list updates and DoCall quits processing poll change notifications when it detects pending poll list updates.

Fixed with commit 6f56f29.

Original Issue

The large default transfer size for disk accesses leads to bad throughput in the DL11 emulation for low speed links, like the 460kBaud the S3board is limited to. Will be overcome by a DL11 controller with more buffering.

Fix

Fixed Resolved with buffered DL11 in commit 1c9dbeb.

V0.50-10 {issue #20} -- DL11: output chars lost when device polling used

Original Issue

Part of the console output can be lost when xxdp test eqkce1 is run on FPGA, also some kernel messages during the 2.11bsd boot sequence. In both cases very simple polling output routines are used. Most likely cause is that device ready polls timeout before the rlink interface can serve the output request.

Fix

Is overcome with buffered DL11 controller with much higher throughput and improved interrupt rate control.

Fixed with commit 1c9dbeb.

V0.77-1 {issue #19} -- tcl getters accessing a const reference crash with a SIGSEGV

Original Issue

tcl commands like

  cpu0 get type
  cpu0rka get class
  rlc get timeout

crash with a SIGSEGV. Apparently all getters which internally return a const reference are affected. Observed with gcc 5.4.0. Unclear whether this is a coding bug introduced when boost::bind was replaced by lambdas (in commit 1620ee3) or a compiler issue.

Fix

The culprit was that automatic return type determination for the getter lambdas was used. This fails when the called method returns a reference of an object. The deduced lambda return type will the object, not a reference. Unfortunately this doesn't lead to a compile time error but to a run time error.

Bottom lime is

  • automatic return type detection for lambda's can be error prone
  • it is safer and also more compact to use std:bind as method forwarder

Fixed with commit 6024dce.

V0.73-3 {issue #11} -- dmscnt and dmcmon disabled in Vivado based flows

Original Issue

The 'state number generator' code in pdp11_sequencer causes in Vivado 2016.1 (and .2) that the main FSM isn't re-coded anymore, which has high impact on achievable clock rate. The two optional debug units depending on the state number, dmscnt and dmcmon, are therefore currently deactivated in all Artix based systems (but are available on all Spartan based systems).

Fix

At least mitigated with d14626c which allows to use dmcmon without the full state number generation logic in pdp11_sequencer. Reintroduced dmcmon in sys_w11a_n4 again. dmscnt is still deconfigured for Vivado designs, but this has much less practical impact.

Closed issues

V0.73-1 {issue #9} -- Vivado xelab sometimes extremely slow

Original Issue

as of Vivado 2016.2 xelab shows sometimes extremely long build times, especially for generated post-synthesis VHDL models. But also building a behavioral simulation for a w11a design can take 25 min. Even though post-synthesis or post-routing models are now generated in Verilog working with xsim is cumbersome and time consuming.

Reason for closure on 2022-07-05

Re-checked with Vivado 2022.1. Building models with xelab is now quite fast. The issue disappeared somewhere between Vivado 2016.3 and 2022.1.

V0.76-2 {issue #17} -- Help wanted: Testing with Arty S7 appreciated

Original Issue

The w11a design for Arty S7 (50 die size), see rtl/sys_gen/w11a/artys7, was provided to support also an up-to-date Spartan-7 based board. Turned out that speed is equivalent to Artix-7. It is so far only simulation tested.

Testing done with a real Arty S7, would be highly appreciated. Please double check the pin assignments (see mig_a.prj and artys7*.xdc) with the documentation of your board to avoid potential damage.

Looking forward to receive test reports.

Reason for closure on 2020-04-20

Apparently nobody invested into an Arty S7. The sys_w11a_as7 will be marked untested, removed from the default build and test flows, but kept in the repository.